Cash · MTD
$358K
AR $184K · $38K past 45d
Pace vs target
$412K
$1.25M target · day 10On pace +$9K
Margin / job
38.4%
36.2% low mid-Jun · recovering
Crews in field
9of 11
9 open WOs · 2 at yard
AI · attention
Bar-D $23K past 60d — draft ready
Crew 9 idle tomorrow — 9 open
CR-2201 stuck en route — 14 hrs
Revenue per crew-day
12 weeks
Rev / crew-day
Target $2.8K
Table
Field map
Pad
Job
C# Crew
Yard
Table
| WO | Lease | Operator | Crew | Stage |
| CR-2209 | Holliday Creek 4-9 | Redfork Energy | Crew 3 | On site — fishing |
| CR-2214 | Bar-D 11 | Bar-D Operating | Crew 5 | Assigned |
| CR-2201 | Kadane A-7 | Kadane Petroleum | Crew 2 | En route — flagged |
| CR-2198 | Electra Fee 22 | Wagoner Oil | Crew 2 | Hot oiling |
| CR-2196 | Scotland Unit 9 | Redfork Energy | — | Complete — monitoring |
Pump status
-
Holliday Creek 4-9Redfork Energy · AFE 26-117
— SPM · 0%
● Down — fishing
-
Scotland Unit 9Redfork Energy · AFE 26-098
8.6 SPM · 71%
● Watch — restarted
-
Kadane A-7Kadane Petroleum · AFE 26-109
7.8 SPM · 96%
● Paraffin — hot oil due
-
Bar-D 14-3HBar-D Operating · AFE 26-104
9.2 SPM · 98%
● Pumping
Overnight log
2 of 11
-
5:12 AMCREW 3
Holliday Creek 4-9 — rods parted, fishing.
AIRedfork notified · parts run 7:00 AM
-
4:38 AMINTAKE
Bar-D 11 down — no flow.
AICR-2214 logged · Crew 5 first light